波音737MAX 9型客机
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机舱应急门脱落、放行问题飞机……波音因“存在数百项质量体系违规行为”,面临高额罚款
Mei Ri Jing Ji Xin Wen· 2025-09-14 02:13
Core Points - The Federal Aviation Administration (FAA) plans to impose a fine of approximately $3.1 million on Boeing due to safety violations occurring between September 2023 and February 2024 [1][3] - Boeing's safety violations include an incident on January 5, 2024, where an emergency door fell off a Boeing 737 MAX aircraft, and interference with the independent duties of safety personnel [1][3] - The FAA's investigation revealed hundreds of quality system violations at Boeing's 737 factory in Renton, Washington, and at a supplier's facility in Wichita, Kansas [1][3] - Boeing has applied for airworthiness certification for two aircraft that do not meet airworthiness standards [1][3] Financial Performance - Boeing reported second-quarter revenues of $22.75 billion, a 35% increase from $16.87 billion in the same period last year [4] - The company experienced a net loss of $612 million in the second quarter, an improvement from a net loss of $1.44 billion in the previous year [4] - Boeing's operating cash flow was $227 million, a significant recovery from a negative cash flow of $3.92 billion in the same quarter last year [4] - The company is facing ongoing financial challenges, including a $445 million payment related to agreements with the U.S. Department of Justice concerning two fatal crashes involving the 737 MAX series [4][5] Regulatory and Certification Issues - The FAA has given Boeing 30 days to respond to the penalty notification [3] - The certification work for the 737 MAX 7 and MAX 10 aircraft, originally scheduled for completion this year, may be delayed until 2026 [5]
波音因安全违规面临美监管机构310万美元罚款
Xin Hua She· 2025-09-13 07:45
Core Points - The Federal Aviation Administration (FAA) plans to impose a fine of approximately $3.1 million on Boeing due to safety violations occurring between September 2023 and February 2024 [1] - The violations include an incident on January 5, 2024, where an emergency door seal fell off a Boeing 737 MAX 9 aircraft shortly after takeoff, and interference with the independent duties of safety personnel [1] - Boeing's facilities in Renton, Washington, and its supplier, Spirit AeroSystems in Wichita, Kansas, were found to have hundreds of quality system violations [1] Company Summary - Boeing has applied for airworthiness certification for two aircraft that do not meet airworthiness standards [1] - An employee at Boeing reportedly pressured internal airworthiness verification personnel to approve the release of a problematic Boeing 737 MAX aircraft to meet delivery schedules [1] - Following the FAA's notice of penalty, Boeing has 30 days to respond [1] Incident Details - The incident involving the Alaska Airlines Boeing 737 MAX 9 occurred shortly after takeoff, with a door seal falling off due to four missing bolts that were supposed to secure it [1] - The aircraft was delivered to Alaska Airlines only about two months prior to the incident [1]
【环球财经】调查显示波音和监管机构在客机“掉门”事故中均有责任
Xin Hua She· 2025-06-25 14:50
Core Points - The National Transportation Safety Board (NTSB) voted to approve the final investigation report on the Boeing door latch incident, highlighting insufficient employee training, guidance, and oversight by Boeing, as well as regulatory failures by the Federal Aviation Administration (FAA) [2][3] - The incident involved a Boeing 737 MAX 9 operated by Alaska Airlines, where a door latch fell off shortly after takeoff due to missing bolts that should have secured it [2] - The NTSB chair stated that the safety deficiencies leading to the incident were preventable and should have been obvious to both Boeing and the FAA, indicating a systemic failure [2] Summary by Sections Incident Details - On January 5, 2024, a Boeing 737 MAX 9 operated by Alaska Airlines experienced a door latch drop shortly after takeoff, with four bolts missing that were supposed to secure the latch [2] - The aircraft was delivered to Alaska Airlines only about two months prior to the incident [2] Findings on Boeing - The investigation found that Boeing failed to provide adequate training, guidance, and oversight to ensure manufacturing personnel consistently followed proper procedures [2] - The missing bolts likely caused the door latch to loosen during previous flights before ultimately falling off [2] Findings on FAA - The report criticized the FAA for its lack of effective compliance oversight and audit planning, which failed to identify and ensure Boeing addressed issues related to its parts removal processes [3] - The FAA acknowledged the report and stated that it has fundamentally changed its regulatory approach to Boeing since the incident, committing to stronger oversight [3] Company Responses - Boeing expressed regret over the incident and committed to improving safety and quality across all its operations [3]