特种设备安全检验
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湖北特检院黄石分院以“硬核”技术实力护航企业安全生产
Xin Lang Cai Jing· 2026-02-10 04:37
Core Insights - The inspection by Hubei Special Inspection Institute's Huangshi branch successfully identified safety hazards in a steel plant's heat storage device, which had exceeded its design lifespan of 10 years, thus ensuring safe production for the enterprise [1][2] Group 1: Inspection Findings - The heat storage device has a volume of 150 cubic meters and was put into operation in July 2011, with a design pressure of 2.65 MPa and a design temperature of 250 degrees Celsius [1] - The inspection revealed fatigue cracks in the circumferential welds between the internal supports and pads, caused by alternating stress from thermal expansion and contraction during operation [1] - Additional issues included multiple mechanical damages on the inner wall of the container and several leaks in the heat exchange tubes, all of which posed significant safety risks [1] Group 2: Remedial Actions - Inspectors communicated with the enterprise's technical head to analyze the defects and develop a scientific rectification plan [2] - The remediation involved grinding and welding the fatigue cracks, followed by magnetic particle testing to ensure weld quality, as well as professional grinding of mechanical damage and individual welding of leaking heat exchange tubes [2] - All defects were rectified according to regulations, and subsequent inspections confirmed that the equipment met safety operation standards, successfully eliminating the safety hazards [2] Group 3: Future Directions - The Huangshi branch emphasizes the importance of special equipment safety, focusing on inspections of aging and high-risk equipment [2] - The institute aims to enhance technical services for key enterprises and high-risk devices, leveraging professional expertise to support safe production and strengthen the safety framework for special equipment in the region [2]
湖北特检院宜昌分院强化“三精”举措护航化工企业设备安全
Zhong Guo Zhi Liang Xin Wen Wang· 2025-10-10 09:08
Core Viewpoint - The inspection team from Hubei Special Inspection Institute's Yichang branch successfully completed the inspection of over 5,000 meters of pressure pipelines at Angel Yeast (Yichang) Co., Ltd., minimizing production losses and ensuring safety standards are met [1][2][3] Group 1: Inspection Preparation - Angel Yeast is a leading company in the global yeast industry, and the steam pipelines under inspection are critical to its main production workshops [1] - The inspection team prepared in advance to assess the operational status, layout, and potential risk points of the pipelines, aiming to reduce the planned 10-day shutdown that would incur daily losses of approximately 5 million yuan [1] Group 2: Quality Control During Inspection - The inspection team utilized various non-destructive testing methods, including digital radiography, magnetic particle testing, and penetrant testing, to examine critical areas such as weld seams and joints [2] - The team emphasized the importance of precision in inspection, stating that every data point and detail is crucial for safety, completing the entire inspection in just 5 days despite challenging conditions [2] Group 3: Safety Measures and Recommendations - The inspection successfully identified and eliminated multiple potential safety hazards, such as localized thinning of the pipelines, and provided targeted rectification suggestions to the company's technical staff [3] - The efficient inspection process not only reduced production losses but also highlighted the dedication and resilience of the inspection team, which will continue to focus on safety needs in key sectors like chemicals [3]